Delay after alarm puts California spill response in question

Delay after alarm puts California spill response in question

SeattlePI.com

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Amplify Energy’s emergency response plan for a major oil spill like the one it’s now dealing with in coastal Southern California depended heavily on a quick shutdown of the San Pedro Bay Pipeline if its sensors picked up a sudden loss of pressure. That’s not what happened, investigators revealed Tuesday.

After an alarm went off in a company control room at 2:30 a.m. Saturday — signaling a rupture that would spill tens of thousands of gallons of crude into the Pacific Ocean — the company waited more than three hours to shut down the pipeline, at 6:01 a.m., according to preliminary findings of an investigation into the spill.

The Houston-based company took another three hours to notify the U.S. Coast Guard's National Response Center for oil spills, investigators said, further slowing the response to an accident for which Amplify workers spent years preparing.

“How come it took so long? That’s a fair question,” said Richard Kuprewicz, a pipeline consultant and private accident investigator from Redmond, Washington. “If you have any doubt, your action should be to shut down and close. ... Something’s not quite right here.”

Pipeline control room alarms don’t always mean a leak and can be tripped by numerous factors — from a faulty signal from a sensor along the line, to a pump that goes offline and causes a sudden pressure change, according to Kuprewicz and other industry experts. But the alarms also are supposed to trigger immediate follow-up actions to quickly ascertain if anything is wrong.

It’s uncertain why that process dragged out hours in San Pedro Bay, potentially worsening a spill that left some birds coated with oil and has stirred worries about broader environmental impacts.

The cause of the pipeline break just offshore from Los Angeles remains under...

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